It seemed innocent enough at the time. I was referred to a
new customer who had a relatively low miles CB200T street bike that was set
aside after extensive carb and petcock cleaning hadn’t solved the bike’s
running problems. Apart from a new coil installed there were apparently no
other modifications done to the machine other than a set of EMGO mufflers that
replaced the rust-prone originals. How hard to it be to get it running again?
It had been sitting for close to a year, apparently, so the
battery was stone-dead and needing replacement. Once the neglected machine was
brought back to the shop, a new battery and some spark plugs were picked up at
the local dealership and a few checks made on the overall condition of the bike
and engine. The compression readings were both right about 150 psi, which
is on the low end of specifications, but should have been good enough to make
it run okay. These are not overly-powerful machines, but should run up to
redline in lower gears without issues.
After experiencing a “wrong coil” issue
with a CR93 Tribute bike a year ago, the first thing to check, once the fuel
tank was removed, was the new ignition coil. Honda’s OEM coils are no longer
available, so you have to go with the only available options; new aftermarket
coils made in China.
Sure enough, when the coil was checked with an ohmmeter, the
primary side resistance was 1.5 ohms, instead of the normal 4.5 ohm readings
for a bike with points and condenser ignition systems. I ordered a correct 4.5
ohm coil and looked over the fuel system while I waited for the ignition coil
to arrive from SFO distributor 4int1.com
I expected to see a set of reversed carburetor slides as a
possible contributor to the reported problems, however they had been installed
correctly. The needle clips were in the middle position and the needles were K
marked OEM parts. Very often carb overhauls are done with aftermarket branded
kits which have poorly engineered replacement parts, but this was not the case
here. Despite laying up for many months the carbs and fuel tank petcock were
still fairly clean and not obviously causing problems.
When the coil arrived, I installed it and screwed the spark
plug caps into the wire ends, which were NGK branded parts. The bike fired up
with the new battery, even on the old fuel, but the engine stuttered and balked
as the throttles were opened much past half way. The engine sounded like it was
choking from excessive fuel, so it was shut back off and the float bowls
removed for inspection of float levels and any blocked air passages. The right
side bowl came off only to find the idle jet lying in the bottom of the bowl!
That explained the over-rich condition that had carboned up the spark plug on
that side. The jet was reinstalled and fresh spark plugs installed. The bike
restarted, sounding better, but still had a mid-range stumble. The plugs were
removed for another look and it appeared that the engine was still running
somewhat rich. When the plug cap was removed, I was startled to see that the
inside of the spark plug cap hardware was still stuck to the end of the spark
plug! Well, that would explain some misfiring!
These small Honda twins have a single, dual-lead ignition
coil, so both spark plugs and caps must be secured to the spark plugs in order
to fire properly. An open circuit on one end or the other causes the spark to
break down immediately. New plug caps were purchased and installed after the
plugs were cleaned and the bike restarted once again. More blubbering sounds
were apparent and this time the left side carburetor’s idle jet was discovered to
have had unscrewed itself and was lying in the bottom of the float bowl! The
jet was still open, so was reinstalled again and the start-up routine repeated.
The bike would start and run okay, but continued to mis-fire beyond mid-range
throttle openings. Now what???
Going back through the ignition system, I checked the
ignition points contact faces, which were a little dished from wear, so they
were cleaned up and re-gapped to specifications. The spark advancer was checked
for proper advance/retard functions and some point cam lube applied to the
advancer cam surface. The ignition timing was reset to the F mark and checked
on both lobes of the point cam. The opening of the points was within a degree
or two of each other, so well within reason. The voltage was checked on the
points when the engine was off and then running. Initially the point voltage
readings were around 9 volts, but then climbed back up towards 12 volts as the
engine speeds were increased. Typically, the ignition voltage should be close to
battery voltage, however these 1975 and later twins have “always ON”
headlights, so there is an immediate voltage draw when the ignition switch is
turned to the ON position.
I opened up the headlight shell to check the wiring color
matches and found the black/white stripe power lead for the kill switch (which
feeds the coil) plugged into a rogue brown wire, normally used for lighting
purposes. Shifting the wire back into the 4 way black connector gave a better
voltage reading, however the headlight feed was also plugged into that
junction. The right side handlebar switch was not the correct one for this
application and normally has a blue white stripe feed going into and out of
that side. The wiring was not present in the switch, so the feed wire had to be
plugged into the main switched black wiring junctions, as well.
The bike was test-ridden numerous times in the local area,
but no matter whether it was going downhill or uphill under load, the same
high-speed cut-out misfiring remained. I
rechecked the fuel and ignition systems once again, eventually replacing the
ignition points and condenser, although they really didn’t appear to be
defective. Most of these components are relatively inexpensive, but I don’t
like to keep throwing new parts into a bike as a process of elimination to cure
a problem. After many hours of checking and rechecking everything from the gas
cap venting to possible muffler back pressure issues, nothing new was found.
The remaining clue was that when a dynamic timing light was connected to the
spark plug wires, the light flashes started to become intermittent when the
engine began the mis-firing routine again. Despite the presence of a “new”
ignition coil of the correct impedance, the symptoms continued to indicate a
failing secondary voltage issue at the plugs.
In desperation, a hopefully good used OEM Honda CB200T coil
was purchased from eBay sellers to prove or disprove whether the misfiring is
still coming from the coil or some as yet undiscovered nuance which has not
been recognized. The coil arrived in just a couple of days and I was holding my
breath about whether this really was the final solution to the mysterious
misfire…. Honda coil installed and the bike went right to redline without any
hesitation….. a LONG and winding road leading to my first inclination that the
“new coil” from China was not up to specs. Apparently of the 100 or so that
4into1 has sold, I got the bad one!
Well the bike has been gone over with a fine-tooth comb and
is now ready to return to its owner, ready and raring to go once again. There
is no way I can get reimbursed for all of my time expended on this repair, but
I have the knowledge that my troubleshooting observations were ultimately
correct. Another day at the office at Casa del Honda.
Bill Silver aka MrHonda
If I remember, with those 2in1 coils if the coil leads were not solidly connected to the spark plugs and they were not tightly secured to the head the coil could sometimes short out internally while trying to fire the other spark plug. What do you think?
ReplyDeleteI had originally reused the NGK caps that were on the bike with the 1.5 ohm coil installed. After installing the 4.5 ohm coil, I did have the spark plug cap come apart internally, but I think it might have still been able to jump the gap. The plugs always came out clean after the carb jets were secured, so it looked like both were firing all the time, but with a WOT high voltage demand, the coil apparently shorted out or arced internally. Marty said they were getting new coils from another supplier soon, but hadn't had any reports of failures in the older ones.
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