The
past few months, it seems that all the local lame and wounded vintage
Hondas have found their way to my little messy shop for repair and
rejuvenation. Having been embroiled in a pair of “beach bike”
CB350s, suddenly a sad, but salvageable later-model CB77 pops on
Facebook forums as a project bike with a seriously seized engine.
Seller was taking offers and finally settled on mine. All I had to do
is drive 150 miles up the road to fetch it and bring home the remains
for revival. Very few CB77s have shown up in SoCal in the past year,
so I guess you have to go out and haul them in if you want to own one
again.
I
already have my low-budget 1963 CB77, which was a bike I pieced
together 6-7 years ago, then let it go to a woman who lost her garage
space and sold it to her girlfriend. She rode it out to Joshua Tree
from San Diego on a woman’s ride, making the journey safely, but
the bike was seeping oil out of the tachometer cable seal and she
parked it in 2016. I wound up buying it back and putting it back into
regular service now and was happy to have it for my runs to the post
office and local trips.
Over
the past year or so, I have snagged bits and pieces of Super Hawks,
either to keep for emergencies or to put a little stash together in
case a bike like this new one shows up for repairs. I have collected
a kickstarter cover, cylinders, cylinder heads, valves, wiring
harness and NOS ignition switch along with a lot of other little
tidbits. So, now it looks like they will be put into play for the
latest project.
The
pickup adventure…
Leaving
at 8:30 AM gave me about 3 hours to cover 150 miles up to and beyond
LA. Waze GPS app took me off the I-5 once, across the 91W to the
605N, then back to the I-5 again. I have learned to trust it and sure
enough, the bulk of the journey north went smoothly and I was there
in 3 hours flat.
I
gave the bike a quick once-over, noting that the cylinders were full
of rust and the tank had stalactites inside once the cap was removed.
It would appear that the cap was left off and the bike left outside
to collect rainwater, which flowed into the open petcock, filled the
carburetor bowls, then traveled down the right side cylinder’s open
intake valve.
The
bike only had 12k miles showing and was a 18K series 1965 model with
an array of little mods including chromed fenders (front one chopped
off), chromed side covers, transmission cover, footpegs and horn
cover. The bike did have OEM exhaust pipes, but one muffler looked
rusted out on the inside, also on the right side.
We
loaded it up, I left a copy of my Classic Honda Motorcycles for Dave
and the shop guys and hit the highway once again. The return leg had
me headed down the I-5, then east on the I-10, then down the 710,
then back to the I-5 again. In the end, the Tacoma covered 340 miles
in 6.15 hours getting 26.4 mpg on the way as we tooled down the
highway at 80 mph for much of the return trip.
Once
the bike was unloaded, I hauled the engine up on the workbench and
filled the cylinders first with Metal Rescue and Kroil, but switched
to straight Metal Prep (phosphoric acid) after trying to loosen the
pistons with my little steering wheel puller (as a pusher) tool
attempt.
How it started out...
The
next day…
Popping
the float bowls off the carburetors revealed massive amounts of water
damage corrosion to both carbs and the petcock. Metal was etched away
on one carb main jet holder area and the petcock had a pinhole at the
top where the metal had been eaten away. Fortunately, I had a spare
set of square bowl carburetor bodies that should be good enough to
bring the bike back to life again, once everything is put back
together.
I
ordered $100 worth of bits from 4into1.com and a new AGM MotoBatt
battery from an eBay supplier.
I
filled the gas tank with ¾ gallon of Metal Prep, let it sit for
awhile then added water to the top opening and will let it sit for a
few days. Hopefully, the pistons will loosen up and I can continue
with the engine rebuild without resorting to violence on the piston
crowns.
The
worst one ever…
Using
my steering wheel puller tool as a piston pusher, the pistons refused
to budge, especially the left side one which was near TDC. The right
side finally moved slightly, which just raised the cylinders off the
crankcases ever so slightly. More pressure on the left side resulted
in a loud crack and the top of the cylinder liner snapped off. The
liner/piston combo could only go down so far before hitting the
crankshaft, so this strategy wasn’t really working out. All I could
do was totally destroy the cylinder block in order to remove the
pistons from the crankshaft.
First,
I took a hacksaw and sawed the cylinder block in half through the
camchain cavity. Then, I had to pull the whole bottom end off the
bench and over to my air compressor where I used an air chisel to
pound out the right side piston from the sleeve. Next, the left side
sleeve was pushed off the cylinder casting, leaving it intact and
hanging from the connecting rod. I gathered it back up and put it
back on the workbench, then attacked the sleeve with a Dremel tool
with a cutoff wheel(s). Cutting down both sides of the sleeve about
halfway allowed me to split the sleeve with a chisel, revealing a
fully rusted piston from top to bottom and rust below the piston in
the sleeve as well. I have never seen so much corrosion buildup
between the piston and sleeve on a water-seized engine before.
The
piston was finally clear of the cylinder sleeve, but we weren’t
done just yet! Using a very big piston pin pusher tool, the pin was
stubbornly stuck in the piston pin bores. I had to break out the
Dremel tool again and cut the piston apart through the pin bore which
finally relaxed enough to release the pin and the rest of the piston.
I figure that it took about 6 hours of labor just to remove the
pistons and cylinders from the crankcase and crankshaft. Worst one
ever….
The
cylinder head combustion chamber on the right side was pitted from
years of standing water on that side, so it went to the scrap heap,
as well. I continued to dismantle the rest of the engine in order to
clean out all the debris from the piston removal process and check
over the transmission and kickstarter parts. Fortunately, the bottom
end was pretty clean and just needed a lot of washing of parts in
order to clear the leftovers from the piston destruction process.
The
whole outside of the engine was covered in layers of grease, dirt,
oil, corrosion that took plenty of time just to scrape off the worst
of it. I discovered a local shop that had a vapor blaster machine
and was willing to clean the parts properly. Everything came back
looking like fresh alloy, but needed a second cleaning/rinsing to
clear leftover glass bead debris from the cleaning process. Now I
could start to rebuild the engine using nice clean parts.
The
spare cylinder head had good seats for the valves, only needing a
little pass with the valve seat cutters to make nice shiny little
circles in the cast-iron skull that comprises the combustion chamber,
valve seats and spark plug hole. I installed a new set of valves with
the original valve springs which had blue paint on the ends, which I
had never noticed before on CB engines.
The
spare cylinders on hand were still at STD bore, but one side had a
single scratch down the side, but below the top couple of inches of
piston travel. I cleaned up a set of STD pistons and rings that were
hiding in a box and set about putting the whole top end back together
with replacement parts from stock. The bottom end really didn’t
need much in the way of replacements, apart from the kickstarter pawl
which was somewhat rounded off on the contact surface.
Reassembly
of these engines takes more time than you would expect, especially
when each part needs to be cleaned and evaluated for re-use. I spent
a couple of afternoons cleaning and assembling all the bits and
pieces until I had a gleaming shiny engine assembly sitting on the
bench. Next step, the chassis..
I
spent a good part of a day first removing the front wheel and forks
in order to replace the left side upper fork ear, which was flattened
out from some impact. I was able to get a NOS part from
www.davidsilverspares.com for $65, which came in factory primer, so
needed a coat of black paint to match the rest of the bike. While
apart, I cleaned the fork seal holders and the chromed trim rings
which had some pitting, but were good enough for the moment.
Invariably,
the brake cams on these bikes are all sticky from 50-year-old grease
and the intrusion of moisture over the years, so they must be
dismantled, cleaned and lubricated. Honda didn’t make it very easy
to dismantle the brake plates, as the brake shoe pivot bolts are held
into the plate with nuts on the outside which have little punch mark
stakes in two places. There is no room to get a socket onto the nuts,
so I went in from the backside and used an air tool to break the
19mm head bolts loose from the 17mm nuts on the outside. Once apart,
I replaced the front shoes with new aftermarket Vesrah brand
replacements, which are non-asbestos materials. The original 5mm shoe
thickness was worn down to about 4.3mm on the front and 3.4mm on the
rears. I wound up using the used front shoes on the rear brakes in
the end.
Both
brake drums were rusted, as expected, but a half hour of cleaning
with a drill motor and small wire wheel eventually removes all the
rust and scale from the drums. More time was spent cleaning the rims
with 0000 steel wool, just to make them look a little more
presentable. The whole bike was just dirty and corroded to a degree,
but Honda’s chrome was of pretty good quality and a lot of the
original finishes came back up pretty well.
The
bobbed front fender, which had been chromed was a problem to solve. I
discovered an eBay vendor who had some of the Japanese made
replacement fenders which I have seen before on other bikes in the
past. The front fenders on CBs come in two versions, depending upon
how they mount to the forks. This early bike has the steel fork
sliders, so needs the early hockey stick type of center mounting
ears. I knew that it wasn’t really the best option but at $100 it
seemed like a good temporary fix for the front fender situation. The
fender arrived quickly, but the troubles were just beginning.
For
all appearances, the fender should have bolted up to the forks, as
planned, but when the locating pins were pushed into the fender stay
pads, the bolt holes were off about half a hole diameter. Well, that
was weird, but perhaps they just had a bad day at the factory back
then, I thought. Unfortunately, the more I whittled on the fender
mounting hardware, the more it seemed like this was really NOT
designed for this bike! The fender sits up about 2” above the tire
and neither of the fender stays come within 2” of connecting to the
fork slider. The curvature seems a little off, as well, perhaps due
to the possibility that the fender was designed for a 19” wheel not
the 18” wheel of a CB77. So, I really don’t know what this fender
was destined for but it doesn’t appear to be for a Super Hawk
model. The only other fender of that type of mounting system is the
early CB450K0 Black Bombers, but I was never aware that there were
aftermarket fenders designed for that model. So, no I am stuck with
an ugly $100 fender that doesn’t work at all on this bike and is so
carved up that it can’t be returned now. Interesting lesson learned
here…
Next
up, the marriage…
The
chassis needed a good scrubbing to clear off years of dirt, oil and
corrosion, so it got a good bath before the engine was reinstalled
into its original place. Once cleaned off, there are still many
hours of work to do in order to make this machine come back to life
again.
As
in interesting sidelight, the guy who did my vapor blasting had a
black CB77 rolling chassis with motor sitting on a second level floor, just kind of hanging out there. It had a seat and fuel
tank, which I needed for the LA bike, so I asked about it. The owner
said, “You sold me that bike for $100 years ago and you can have it
back for $100.” So, I added $100 to the bill and brought back yet
another CB77 to make it a trio at the house for now.
Fired
up, but leaking oil…
The
engine started up on the first few turns, coughing and smoking out
the mufflers for a few minutes. A few oil drips showed up quickly on
both cylinder head covers, probably due to my reuse of the parts that
still had the original gaskets. They looked good enough to reuse, but
they were hard and just didn’t seal well. I replaced both cover
gaskets, which cured the oil leaks there, but a more serious one
materialized at the middle of the brand new head gasket. The head
gasket was from an aftermarket company with little dimples across the
surfaces. I don’t know what happened there, but it was
disappointing to see and required another engine removal to replace
the gasket and check the o-rings for sealing. The o-rings are
supposed to be 2mm thick, but some of the aftermarket versions seem
to be closer to 1.75mm. Digging into a Harbor Freight box of Viton
o-rings, I came up with some that were about 2.4mm thick, so I opted
to use those instead. I also coated the inside of the o-ring holes in
the head gasket with some liquid sealer to prevent oil migration
laterally through the gasket material. I coated the gasket with
Gasket-Cinch and let it set up before installing the gasket and
cylinder head.
Using
a hydraulic bike lift to help handle the engine assembly made it a
bit easier on my aging spine, but I still have to lift it up/down
about a foot from the bench to the lift. I always feel it the next
day or two, though. It winds up being a good 3-4 hour job to manually
dismantle the bike’s external parts and ease the motor down and out
of the frame. A good hour or so was spent on the bench, dismantling
the cylinder head from the engine and cleaning, inspecting, gasket
scraping, and prepping the parts for reassembly. Then, it is back onto
the lift and back over to the frame. Unlike the Scramblers, the Super
Hawk engines go straight up into the frame from the bottom, so
jockeying it around and into the mounting points is much less of a
strain on the old bones.
Fired
up 2.0...
Once
the bike was nearly back together again, the engine was test-fired to
verify that the head gasket leak was solved and everything was back
to specs again. For almost all of the CB77s that have come my way, I
have installed #140 main jets to compensate for the alcohol in
today’s fuel supplies. This setup in my 1963 CB77 works flawlessly,
with easy cold starts and smooth fuel delivery all the way to
redline. This 1965 bike wasn’t having any of that...
First, the bike sounded like it was running very rich at mid-range and
spitting back through the left carburetor off-idle, which is a
confusing combination of symptoms. I discovered that once the fuel
tank was cinched down onto the frame, apparently the throttle cable
was getting pinched off somehow and the carb synch was WAY OFF. The
left side was lifting 1/4” before the right side started up. It
wasn’t making much sense as the new cable was used and the carb
slides and adjusters were matching height at first. When the fuel
tank was loosened up, the carb synch issues swapped sides! Pushing
the parts around finally got the cables to match up normally and the
carb synch was restored. I had installed a set of OEM carb needles
and have moved the needle clips up and down, trying to find the happy
place for the engine.
Finally,
I swapped out the #140 mains for a set of stock #135s and the engine
began to smooth out through the rev range. The ignition timing was
rechecked using an automotive timing light and it was discovered that
when both sides were setup at the F mark at idle, the wear inside of
the camsprocket advancer weight pads have compressed somewhat which
creates excessive spark timing at full advance. I have found that you
MUST contain the spark advance to stay close to the II marks on the
rotor at full advance. Setting the spark advance timing to that limit
yielded idle spark timing at the T mark instead of the F mark.
My
friend Tim Miller, down in TX, dismantles the camsprockets and
modifies the spark advance curves so that they have about 10 degrees
less total timing advance, but this allows the engines to run about
10 degrees BTDC at idle, which is where they really like to be. If
the engine has to come down again in the future, I will ship the
camsprocket out to Tim for rebuilding.
A
few local test rides are showing promise as the engine beds in and
the carbon and oil is all burned out of the exhaust system. The
engine compression readings are right at 160 psi on both sides, which
is about normal for the later lower compression piston setups that
Honda used after 1965.
Some
of the big-ticket items for this revival included nearly $400 just
for vapor blasting the engine components, $65 for the AGM battery,
then another $50 just for the battery hold-down plate and cushion,
$60 for a new drive chain, $65 for a set of mirrors, $155 for a set
of cables to replace the original tach, speedo, clutch, front brake,
rear brake and throttle units. I used the gas tank from the newly
acquired $100 parts bike, which needed a $160 clean and seal, then a
$125 black paint job. I added one of my little Dream 50 tail light
lenses, which are an inch and a half shorter than the regular long
lens used on all of the 1963-66 models. The stock right-side muffler
had a section that was rusted through in one spot which required a
$50 welding job. The speedometer went haywire on the first drive, so
$275 was spent on getting the meters rebuilt at Foreign Speedometer
here in San Diego. I picked up an aftermarket blue seat from my
friend in TN who brought it to the Barber Vintage Festival in Oct.
$90 including shipping back to San Diego. The original seat pan was
poorly repaired with someone with an arc welder, instead of a TIG
welder. Aftermarket copy seat bolts set me back another $20.
The
spare cylinder head got a new set of valves which run about $100, then
gaskets and seals add another $80 to the mix. I already had a spare
set of cylinders, STD pistons/rings that were used but good enough to
put together with confidence. The head and cylinders/pistons would
have run another $250 if I had to purchase them elsewhere. Tim
McDowell supplied a set of aftermarket air filters, air tubes
speedometer packing, and other bits that ran up another $200. The
carburetors needed kit parts and floats, so $80 more to the total.
The new CA title costs $55 plus 2 trips to DMV and one to CHP offices
for inspection and VIN verification appointments. After awhile, you
step back and gasp at all of the money spent just to get a bike like
this from parts bike status to a full running motorcycle again. The
parts bills can easily run to $2k especially if you have to buy new
pistons/rings and then bore the cylinders for $90 to machine two
cylinders. And don’t ask about the hours invested in all the steps
to clean, repair and assemble the whole bike again…
In
the process of rebuilding the bike, which still has the original
paint and all of the extra chromed parts attached, the former owner
of my 1963 bike (which I bought back from her a few months ago) fed
me a referral to an interested buyer for the 1965 bike. He brought
his 12-year-old son with him and even though the bike wasn’t quite
finished, then had a flat tire, but he was enamored with it and
wished to buy it when everything is complete.
So,
in less than 2 months, the very dead CB77 is now back on its
wheels, with a running, rebuilt engine and a promising future with a
new family who plan to keep it as an heirloom to be passed down to
the next generation in years to come. The end result makes all the
labor and expenses worthwhile.
THE END...
Bill
“MrHonda” Silver
11/2021